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In-Situ and Laboratory Investigation on Leaching and Effects of Early Curing of Shotcrete Cover

In-Situ and Laboratory Investigation on Leaching and Effects of Early Curing of Shotcrete

Open Access
|Dec 2019

Abstract

During the construction of a rock tunnel in Stockholm, several sections with leaching shotcrete (sprayed concrete) were found one year after the spraying was completed. An investigation was therefore conducted, and its results are presented in this paper. The amount of leaching after such a short time indicated that a one-sided water pressure existed in combination with a permeable shotcrete. The reason for the water pressure was likely a partly unsuccessful grouting that created sections with leaking water. The permeable shotcrete could be a combined result of insufficient curing and the use of accelerators, and the effect of in-situ curing was therefore investigated. A total of six slabs were sprayed and cured under different conditions in the tunnel. Test results according to standards indicated that curing has no significant effect on the development of mechanical strength or water penetration through the shotcrete. However, this is believed to be a result of the test method rather than the non-existing effect of curing. Lastly, some modifications to the test standard were proposed for future studies of in-situ curing.

DOI: https://doi.org/10.2478/ncr-2019-0014 | Journal eISSN: 2545-2819 | Journal ISSN: 0800-6377
Language: English
Page range: 23 - 37
Submitted on: Mar 14, 2019
Accepted on: Sep 30, 2019
Published on: Dec 31, 2019
Published by: Nordic Concrete Federation
In partnership with: Paradigm Publishing Services
Publication frequency: 2 issues per year

© 2019 Andreas Sjölander, Anders Ansell, published by Nordic Concrete Federation
This work is licensed under the Creative Commons Attribution-NonCommercial-NoDerivatives 3.0 License.